













|
 |
Accidents
| Roseville, Calif. |
April 15, 2003 |
A derailment occurred on the 7 to 30 fan, a group of rails, at the East
end of the Bowl in the Roseville Yard. There were two remote control
engines parked, one in 29 rail and one in 30 rail. The engine that
normally works the City Yard, about 1 mile to the east switching locals,
was moved to the Bowl because the three remotes could not keep up with
the work (Note: three remote jobs replaced two conventional jobs). The
City Yard job was working down the lead on the 16 rail. Another job came
out to go to work and had a problem with their engine. They were
instructed by the Console Herder to take the engine in the 30 rail and
line back for the other job. Not seeing the engine working in 16 rail
they lined back for the engine in 29 rail assuming it was the other job.
This left the 30 rail lead switch lined for 30 rail (Note: 29 rail
switch is off of 30 rail). The City job working in 16 rail was informed
by the Herder that the other job lined behind, assuming the lead was
lined they made a double over to another rail, operating the remote
engine from the vicinity of 16 rail switch. They proceeded up the lead
toward the Pull Back track, running through the 30 rail switch. Then
stopped with a center beam lumber car with one truck over the 30 rail
switch. They started shoving westward for the other rail. The West end
of the lumber car goes back down the lead, the east end and toward 29
rail. As they continued shoving back the lumber car turned sideways and
tipped over landing on the nose of the Unit, Y623, in 29 rail.
Along with the damage to the 30 rail switch and some track damage, five
railcars were derailed. Two of the cars TT2X 86909 and MP 273473 were so
heavily damaged that they were scrapped. The front of Unit Y623 was also
damaged. The damage was said to be at least $60,000. Being this happened
in the middle of Roseville we were very lucky this accident did not
involve hazardous materials.
Could this have been avoided? If there had been an Engineer on board
they probably would have noticed the 30 switch was not properly lined
and stopped short (Rule 6.28). Or, if they didn't notice the switch they
may have heard and felt the engine run through the switch and stopped.
Or, if they didn't notice they had run through the switch the Engineer
may have, while shoving back, felt the cut bogging down and stopped,
there-by reducing the damage. And if there was an Engineer on board they
would have been totally responsible for the accident (Rule 6.28).
|
|
|  |
|